...the car was due to go back to Gary Cook at GDC Automotive for these changes at a later date however an issue with a gear box leak at the end of my rolling road session necessitated this happening sooner....
....my issue turned out to be a porous gearbox end case and required the engine and box out again to fix!

Mad considering the end case was blasted, machined and chromated without anyone spotting a problem and since the gearbox was rebuilt it's sat for the past four years full of oil without an issue and was then used for 400 miles all being good....the rolling road exposed the weakness with a small hole in one corner in what otherwise is a sound end case in good condition! What turned out to be a simple twenty quid weld cost me a bit more!
The saving grace is having good people on my side and big shout out to Gary for taking the car back, resolving the issue as well as completing all the planned modifications without any drama within two weeks! The guy really is legend!
So after collecting the car Wednesday I took it to Nick Fulljames who scared me shitless (the boy sure can drive!) road testing the car and tweaking the engine set-up for road use as planned after the rollers.....
....now absolutely perfect and back home, other than my pending trip to CG, I'm hoping to avoid putting it back on a trailer for the foreseeable!....
Cheers,