OK so probably time for an update.
I left the story having the week-end to fit my sladey-stylin suspension hats. This went OK ready for taking the car down to Centre Gravity on the Monday morning.
I took the hire car and drove back to work, coming back later to meet up with Jon who had his car booked in for the day after
As usual Chris was his usual OCD-brilliance. My car was all over the place when I brought it in and it left beautifully balanced.
Curiously it had lost 50Kg in weight since my last visit - now 1149K with a full tank.
My Sladey-stylin suspension hats lacked one thing - the original version from Elephant racing have some needle-bearing shims - that allow the suspension to rotate freely as the steering is turned. Chris mentioned that without this there is a slight issue with stiction. This has proved to be the case - in the mornging when backing out of the drive it's a bit creaky. Mostly it's not evident when driving but one morning the other week it wanted to turn right for most of the journey, and then left for the last part.
I've not got a solution for this as I've ordered some similar needle-bearing shims in 2.5 inch size, so expect to see this as a future project.
The other thing Chris mentioned was that I'd got a leak from one of the oil pipes in the OSR wheel arch. This was dripping onto the suspension arm but thankfully not hitting the brakes. I made a note to sort this out when I got back from CLM.
At the end of the day (around 7 IIRC) we went out for the test drive. Chris demonstrated how the car tracked true according to the camber of the road. It was feeling great. Then Chris started jerking the throttle on and off, to show that it didn't change direction with a sudden change in balance
"Look - i'm accelerating and braking, accelerating, and braking, accelerating and..... oh shite - your throttle's stopped working" Chris kept it in third and managed to coast around the next roundabout and into a lay by with the engine just on tickover.
He firtled around in the engine compartment
And eventually discovered this
The throttle connecting rod had snapped clean in two. A phone call back to base, and Pete came out. Chris went back and some time later returned with the rod looking like this
Just to be clear he took a stud and drilled out the middle. Then drilled holes in it from the side where the two ends would meet. He then welded it through the holes and at either end - a very strong solution.
I got away at around 8:30pm - once again Chris and Pete went well above and beyond the call of duty.
The car felt great and I enjoyed som spirited driving on the way to and from CLM
Sent from my iPad using Tapatalk