Time for a quick catch up.
My friend Google advised that the handbrake cable outers and the heater flap control outers just came out, so with judicious use of pipe pliers, several splashes of penetrating oil and a lot of cussing and wriggling out they did come.
While I was there, I removed the grommets from around the fuel pipes (front and rear), and out came the pipes, as did the front to rear brake pipe.
I had to cut the fitting off the hard brake pipe that connects to the NS flexible to manage to get them out. Unfortunately the 3-way connectors all look very second-hand, which I had not expected, so they will be replaced, along with most of the hard lines (while I’m in there !)
The wiring fought back strongly, but I finally managed by pushing a little from inside the car, then wriggling a little from the engine bay just ahead of the torsion tube housing, push a bit from inside, pull a bit from outside, repeat until you’ve almost lost the will to live, but finally it all came out. Pulling it over the torsion bar tube was not without swear words, but a lot quicker than getting it out of the rear bulkhead.
That gets me to here (sorry that the ground is in focus, but the bulkhead isn't

)
Then onto the NSR torsion bar.
Loads of penetrating oil, lots of wriggling fore and aft, plenty of cussing and pulling, and finally the outer cover came off. Unfortunately it is rusted at the lower side, so replacement needed. Then it was time for the swing arm part – this took cussing to a new level (or should that be depth). Loads of penetrating oil, levering with bars, hitting and crying did nothing – it just sat there and laughed at me. Time to get creative. I removed the Welch / core plug from the end by cutting a square carefully with a dremel, then levering the residue out. Then came one of my mid-size BFHs, and tapping of the torsion bar deeper into the tube. The torsion bar didn’t go far enough to release the swing arm, but with plenty more levering, swearing, crying, and finally it came free.
There was lots of crud in the lower part of the torsion bar tube, but having cleared it out, everything thankfully looks solid
Now for the torsion bar itself. Well I wriggled, I shook, I cussed some more, but it was resolute. Being scared of scratching the torsion bar, I couldn’t hit it or use mole grips. So, using my best sailing bowlines, I attached it to a slide hammer and shocked it a lot. It took absolutely ages, but in a desperate bid to clutch at any glimmer of hope, I started measuring how far it had moved. Was that a whole mm it had moved, or was I holding the tape measure at a different angle this time. More shocking and yes, it had definitely come out a single mm. More shocking and we went to 2, then 3. With sweat dripping off me, it was time for coffee, then back on with the aerobic work out – hey who needs to go to a gym anyway !. 5mm, then 10, then eventually it was out and I was cream crackered.
Today, for a bit of light relief, I made a start on turning my pair of mobile axle stands into a cradle for transport. I’d bought some steel from my local stockist, including 7.5m length of 40x40x3 rhs. This was chopped up using my man-maths justified new TCT blade chop saw - why had I waited sooo long – it is like a knife through butter. My master plan is to run two lengths of 40x40 front to rear, joining them solidly. I’ve cut 100mm lengths of 50x50x3 rhs to weld to the mobile stands and will clamp the 40x40 into them. I’m intending to make supports that attach to the rear torsion bar mounts and the front sub-frame mounts. For the front I’m using some 50x50x3 angle, but will need to spacers on the forward bolt. This will be welded to a 40x40rhs upright, similar to the original, but longer / taller. Having measured the required distance between the front to back supports, I cut two 2m lengths. This left me with 3.5m to make 4 uprights.
Using some 5mm thick plate and the torsion bar outer cover as a template, brackets were knocked up, then welded to a pair of uprights. Welding 5mm plate to 3mm rhs is new to me, so I cranked up the welder, made a couple of tacks, cranked the welder up a tad more and laid some bead welds. Gosh, it’s so much easier then welding thin sheet !. Then I got cocky and started with the circular motion, leaving my pile of dimes behind. Pretty impressed if I say so myself, but although it will be more than strong enough, probably would get laughed at by a proper coded welder.
Then for some light hearted relief, I temporarily stuck this back on with clamps
Seems like ages since it was in place. Its absence has certainly made access for attacking the torsion bar a lot easier.
The eagle eyed will notice the absence of a torsion bar access hole in the lower wing, but I assure you that this is deliberate. There is a pilot hole in place, but I thought it better to refit the wing and check the hole is in the right place before cutting a big hole – it’s so much harder to move a big hole than a pilot hole.